West Mailisu #2 well update
Posted: 15 August 2011
Caspian Oil & Gas Limited reported the operation to recover the stuck cementing string on its West Mailisu #2 well is progressing according to plan.
As reported on 8 August, problems were encountered setting a cement plug to isolate Bed V from water-bearing sands and the string became stuck.
A total of about 1630m of tubing has been removed from the hole and the remaining ~80m is expected to be removed early this week.
Following this removal, a cement plug will be set at the 7” casing shoe (approximately 1709m) before perforating and flow testing Bed III over a 10m interval with the best sand development (1785-1795m – loggers depth).
Posted by Richard Price, Editor, energyme.com.
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